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So what happened to my old 4G63...
#101
Posted 06 February 2008 - 05:06 AM
he has some good results... but only really good with GTRs and Skylines Nissans in General
Grant
#102
Posted 06 February 2008 - 05:29 AM
conflict
Maybe we should start a conflict section? Where E-men can go man to man and battle it out in a war of keyboard fury...
hahaha
Then we can have
Keyboard warrior of the world championship..
#103
Posted 06 February 2008 - 06:11 AM
#104
Posted 06 February 2008 - 06:26 AM
2.3 Litre Stroker built by Tech//Sport
#105
Posted 06 February 2008 - 07:35 AM
hahahaif my sister looked like that u can keep her
lol
i didnt know you were from tasmania
#106
Posted 04 March 2008 - 10:59 AM
I've had my car to Ray at RE Customs to have the AFR checked and timing done on his dyno, I'd recommend him based on what I've seen of his workshop and the care he took of my car while running it.
#107
Posted 04 March 2008 - 11:56 PM
I did however have the pleasure of meeting him (Bought cooler/piping) and had a brief chat about his engine. unfortunate turn of events really.
#108
Posted 05 March 2008 - 12:29 AM
all 16 valves were fucked.. they had eaten away(rubbed) on the shaft
all 16 valves had detonation marks
afew of the valves had the rear skirts on them fucked (spark plug bit loose)
head had detonation marks around the sealing bore (massive holes, very pitted)
Jon
Current Rides:
My06 Evolution IX 12.11 @ 113mph 252kw (street weight)
1997 Proton Satria GLi (daily)
Previous Rides
1993 Mitsubishi Lancer GSR 4G93T 200kw @ hubs 12.1 @ 115.5mph
1992 Mitsubishi Lancer Evo 1 (CD9A) 225kw, 20g, stock ecu, hks 264s 12.050 @ 116.5mph OHH YERRR
#109
Posted 05 March 2008 - 02:50 AM
here is a little update:
http://4gtuner.com/f...t=8289&start=15
it seems that the intercooler piping had cracked welds on them, which would have caused the turbo to run inefficiently to make the same amount of boost... therefor very hot air and a lean mixture..
this would also be another reason that the engine would have detonated.
iluszn wrote:
Just checked it now.. torch in dark room.
Looks like the welds were just to thin and came through.. If i put it on the car now the pipe would break off me thinks.. ill have to get this section redone. ah well. thems the breaks..
yeah it looks like thin welds.. Ill get it all fixed up.
AMG | http://www.4gtuner.c...mmc-galant-amg/
GVR4 | http://www.4gtuner.c...shi-galant-vr4/
Springy Motors | Autronic | Motec
#110
Posted 05 March 2008 - 02:52 AM
#111
Posted 05 March 2008 - 03:13 AM
he is a good welder, but it looks like they ported it out too much...
AMG | http://www.4gtuner.c...mmc-galant-amg/
GVR4 | http://www.4gtuner.c...shi-galant-vr4/
Springy Motors | Autronic | Motec
#112
Posted 05 March 2008 - 03:35 AM
Oh for anyones interest, The support for the cooler is different between Aspec and Jspec. Have to fit a Jspec one to my car to make the cooler line up correctly.
apart from that, no other complaints , should all go on smoothly.
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